The
top hate of everyone running the continuous dyeing machines was when
the elastic got wrapped round a roller in the steamer. You were usually
alerted by a loud bang, the arms suddenly moving or a loose end suddenly
going through the wash tanks.
To
sort out a wrap was horrible and could take anything between a few
minutes and an hour depending on how bad it was. First you had to stick
your head into a steamer (the sweat absolutely pours out of you) and
find it, then you have to try and cut it out while at the same time
avoiding burning yourself (which was often) on the scalding hot metal
surfaces. It was often at a difficult angle, the elastic was tightly
wrapped and very difficult with scissors. Then finally you had to thread
the machine back up and get it running again.
You
did the job always under the constant threat of this problem. Initially
the top cause is inexperience and running the machine too slack, but
once you have learned to run the machine the number one problem was
knots left in the elastic by the weaving department. Even if they don’t
cause wraps the amount of stoppages they caused was very frustrating.
A
6000 meter order running at 100 meters a minute should obviously take
an hour but frequently took an hour and a half because of this problem.
Once while the machine was down I went through the log book and
calculated the amount of downtime the previous week and it came to over
11 hours.
The
solution to the problem was obvious, all the management had to do was
have a quick meeting with the weavers and tell them all to stop leaving
knots in the web. Even if only half of them listened it would have made a
massive difference to us and the production figures. What they did was
absolutely nothing, despite every operator on every shift complaining
about it for years they barely acknowledged the problem let alone do
anything about it.
I
find it almost impossible to understand why they ignored such an
obvious problem that cost so much in downtime, either they were
completely incompetent or making so much money anyway that it didn’t
matter to them.
Another
example of this mentality were the two idiots employed in the
stockroom, in theory all I had to do was give them the order tickets and
they would bring out the tubs of elastic. What actually happened is
that they did only a fraction of the work they were paid to do. I was
constantly having to go into the stockroom fetching web they wouldn’t
strip from the looms or had told me they didn’t have. By doing this of
course I was leaving my machine and risking wraps (see above). I had
constant arguments with both them and the management about this but
ultimately nothing other than a few words were said about it in seven
years.Tony and Roland were both a blatant insult to the countless people
who want to work but couldn’t find a job. But then again I blame the
management for not doing anything about it rather than them for being
bone idle.
The
third major problem was other machine operators on the other shifts who
left you in a mess. Top of the list by a long margin was Mat Hall, to
put it mildly he was an absolute nightmare. Not looking after the
threader elastic which we used to put a test piece through the machine
was my number one complaint. I probably spent half hour in the steamer a
week because of this alone. Then he wouldn’t leave me any dye/finish
made up or not take his used tubs back into the weaving. As above I made
countless complaints to both him and the management and wrote it in the
logbook on a regular basis but nothing was ever done about it.
I
could write an entire website on the nightmare of working in the
dyehouse but the above 3 examples are enough to illustrate what it was
like. It was just a constant stressful ordeal. Other people complained
about working at Charnwood but their issue was always money as we went
several years without having an annual pay rise.
I
was very unusual in the fact that money was a long way down my list of
employment priorities. I had a low cost lifestyle, lived at home, no car
and no other commitments. I would have been more than happy to have
taken a 20 percent pay cut in exchange for not having to go through what
I have outlined above. Some people have since commented that they
didn’t know how I managed to stick 7 years in that place. Looking back I
should have left after around 3 years as I had enough savings to deal
with a spell of unemployment.
Memories
of the 2 years after leaving school such as being messed about by
employment agencies were still fresh in my mind and thats what kept me
at Charnwood.
I
did everything I possibly could to try and get the management to
listen, sometimes if one of the above problems caused 15 minutes of
downtime I would deliberately make it take longer (say 30 minutes) but
even that didn’t work. I can only conclude that the management were
completely incompetent or the company was making so much money they
could tolerate massive amounts of downtime.
The
only way I could vent my frustration was by refusing to help them
whenever they needed it. I told them many times “you help me and I’ll
help you”. After 2 years I never did any overtime no matter how
desperate they were or how easy the work was. If they sorted out the
above problems they wouldn’t have to get people in at the weekend in the
first place. A couple of times they offered triple pay to work bank
holiday monday……..”not interested”!!!!!!!
I
was getting 20 percent more money for 100 percent more stress than when
I first started. If I had been less enthusiastic or played the idiot I
wouldn’t have been put on the colours machine in the first place………..
No comments:
Post a Comment